22 research outputs found

    Built-In Self-Test for Automatic Analog Frequency Response Measurement

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    Abstract-We present a Built-In Self-Test (BIST) approach based on direct digital synthesizer (DDS) for functional test of analog circuitry in mixed-signal systems. DDS with delta-sigma noise shaping is used to generate test signals with different frequencies and phases. The DDS-based BIST hardware implementation can sweep the frequencies through the interested bands and thus measure the frequency response of the analog circuit. The proposed BIST approach has been implemented in Verilog and synthesized into a Field Programmable Gate Array (FPGA). The actual device under test (DUT) was implemented using a Field Programmable Analog Array (FPAA) to form a complete BIST testbed for analog functional tests

    Precise linear signal generation with nonideal components and deterministic dynamic element matching

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    A dynamic element matching (DEM) approach to ADC testing is introduced. Two variants of this method are introduced and compared; a deterministic DEM method and a random DEM method. With both variants, a highly non-ideal DAC is used to generate an excitation for a DUT that has effective linearity that far exceeds that of the DAC. Simulation results show that both methods can be used for testing of ADCs. The deterministic DEM (DDEM) offers potential for a substantial reduction in the number of samples when compared with a random DEM approach with the same measurement accuracy. It is shown that the concept of usinf DEM for signal generation in a test environment finds applications well-beyond ADC testing. The DDEM approach offers potential for use in both production test and BIST environments

    High-speed Time-interleaved Digital-to-Analog Converter (TI-DAC) for Self-Interference Cancellation Applications

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    Nowadays, the need for higher data-rate is constantly growing to enhance the quality of the daily communication services. The full-duplex (FD) communication is exemplary method doubling the data-rate compared to half-duplex one. However, part of the strong output signal of the transmitter interferes to the receiver-side because they share the same antenna with limited attenuation and, as a result, the receiver’s performance is corrupted. Hence, it is critical to remove the leakage signal from the receiver’s path by designing another block called self-interference cancellation (SIC). The main goal of this dissertation is to develop the SIC block embedded in the current-mode FD receivers. To this end, the regenerated cancellation current signal is fed to the inputs of the base-band filter and after the mixer of a (direct-conversion) current-mode FD receiver. Since the pattern of the transmitter (the digital signal generated by DSP) is known, a high-speed digital-to-Analog converter (DAC) with medium-resolution can perfectly suppress main part of the leakage on the receiver path. A capacitive DAC (CDAC) is chosen among the available solutions because it is compatible with advanced CMOS technology for high-speed application and the medium-resolution designs. Although the main application of the design is to perform the cancellation, it can also be employed as a stand-alone DAC in the Analog (I/Q) transmitter. The SIC circuitry includes a trans-impedance amplifier (TIA), two DACs, high-speed digital circuits, and built-in-self-test section (BIST). According to the available specification for full-duplex communication system, the resolution and working frequency of the CDAC are calculated (designed) equal to 10-bit (3 binary+ 2 binary + 5 thermometric) and 1GHz, respectively. In order to relax the design of the TIA (settling time of the DAC), the CDAC implements using 2-way time-interleaved (TI) manner (the effective SIC frequency equals 2GHz) without using any calibration technique. The CDAC is also developed with the split-capacitor technique to lower the negative effects of the conventional binary-weighted DAC. By adding one extra capacitor on the left-side of the split-capacitor, LSB-side, the value of the split-capacitor can be chosen as an integer value of the unit capacitor. As a result, it largely enhances the linearity of the CADC and cancellation performance. If the block works as a stand-alone DAC with non-TI mode, the digital input code representing a Sinus waveform with an amplitude 1dB less than full-scale and output frequency around 10.74MHz, chosen by coherent sampling rule, then the ENOB, SINAD, SFDR, and output signal are 9.4-bit, 58.2 dB, 68.4dBc, and -9dBV. The simulated value of the |DNL| (static linearity) is also less than 0.7. The similar simulation was done in the SIC mode while the capacitive-array woks in the TI mode and cancellation current is set to the full-scale. Hence, the amount of cancelling the SI signal at the output of the TIA, SNDR, SFDR, SNDRequ. equals 51.3dB, 15.1 dB, 24dBc, 66.4 dB. The designed SIC cannot work as a closed-loop design. The layout was optimally drawn in order to minimize non-linearity, the power-consumption of the decoders, and reduce the complexity of the DAC. By distributing the thermometric cells across the array and using symmetrical switching scheme, the DAC is less subjected to the linear and gradient effect of the oxide. Based on the post-layout simulation results, the deviation of the design after drawing the layout is studied. To compare the results of the schematic and post-layout designs, the exact conditions of simulation above (schematic simulations) are used. When the block works as a stand-alone CDAC, the ENOB, SINAD, SFDR are 8.5-bit, 52.6 dB, 61.3 dBc. The simulated value of the |DNL| (static linearity) is also limited to 1.3. Likewise, the SI signal at the output of the TIA, SNDR, SFDR, SNDRequ. are equal to 44dB, 11.7 dB, 19 dBc, 55.7 dB

    A built-in self-test technique for high speed analog-to-digital converters

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    Fundação para a Ciência e a Tecnologia (FCT) - PhD grant (SFRH/BD/62568/2009

    An embedded tester core for mixed-signal System-on-Chip circuits

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    High-accuracy switched-capacitor techniques applied to filter and ADC design

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    Quiescent current testing of CMOS data converters

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    Power supply quiescent current (IDDQ) testing has been very effective in VLSI circuits designed in CMOS processes detecting physical defects such as open and shorts and bridging defects. However, in sub-micron VLSI circuits, IDDQ is masked by the increased subthreshold (leakage) current of MOSFETs affecting the efficiency of I¬DDQ testing. In this work, an attempt has been made to perform robust IDDQ testing in presence of increased leakage current by suitably modifying some of the test methods normally used in industry. Digital CMOS integrated circuits have been tested successfully using IDDQ and IDDQ methods for physical defects. However, testing of analog circuits is still a problem due to variation in design from one specific application to other. The increased leakage current further complicates not only the design but also testing. Mixed-signal integrated circuits such as the data converters are even more difficult to test because both analog and digital functions are built on the same substrate. We have re-examined both IDDQ and IDDQ methods of testing digital CMOS VLSI circuits and added features to minimize the influence of leakage current. We have designed built-in current sensors (BICS) for on-chip testing of analog and mixed-signal integrated circuits. We have also combined quiescent current testing with oscillation and transient current test techniques to map large number of manufacturing defects on a chip. In testing, we have used a simple method of injecting faults simulating manufacturing defects invented in our VLSI research group. We present design and testing of analog and mixed-signal integrated circuits with on-chip BICS such as an operational amplifier, 12-bit charge scaling architecture based digital-to-analog converter (DAC), 12-bit recycling architecture based analog-to-digital converter (ADC) and operational amplifier with floating gate inputs. The designed circuits are fabricated in 0.5 μm and 1.5 μm n-well CMOS processes and tested. Experimentally observed results of the fabricated devices are compared with simulations from SPICE using MOS level 3 and BSIM3.1 model parameters for 1.5 μm and 0.5 μm n-well CMOS technologies, respectively. We have also explored the possibility of using noise in VLSI circuits for testing defects and present the method we have developed

    Fully digital-compatible built-in self-test solutions to linearity testing of embedded mixed-signal functions

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    Mixed-signal circuits, especially analog-to-digital and digital-to-analog converters, are the most widely used circuitry in electronic systems. In the most of the cases, mixed-signal circuits form the interface between the analog and digital worlds and enable the processing and recovering of the real-world information. Performance of mixed-signal circuits, such as linearity and noise, are then critical to any applications. Conventionally, mixed-signal circuits are tested by mixed-signal automatic test equipment (ATE). However, along with the continuous performance improvement, using conventionally methods increases test costs significantly since it takes much more time to test high-performance parts than low-performance ones and mixed-signal ATE testers could be extremely expensive depending on the test precision they provide. Another factor that makes mixed-signal testing more and more challenging is the advance of the integration level. In the popular system-on-chip applications, mixed-signal circuits are deeply embedded in the systems. With less observability and accessibility, conventionally external test methods can not guarantee the precision of the source signals and evaluations. Test performance is then degraded. This work investigates new methods using digital testers incorporated with on-chip, built-in self-test circuits to test the linearity performance of data converters with less test cost and better test performance. Digital testers are cheap to use since they only offer logic signals with direct connections. The analog sourcing and evaluation capabilities have to be absorbed by the on-chip BIST circuits, which, meanwhile, could benefit the test performance with access to the internal circuit nodes. The main challenge of the digital-compatible BIST methods is to implement the BIST circuits with enough high test performance but with low design complexity and cost. High-resolution data converter testing needs much higher-precision analog source signals and evaluation circuits. However, high-precision analog circuits are conventionally hard to design and costly, and their performance is subject to mismatch errors and process variations and cannot be guaranteed without careful testing. On the digital side, BIST circuits usually conduct procedure control and data processing. To make the BIST solution more universal, the control and processing performed by the digital BIST circuits should be simple and not rely on any complex microcontroller and DSP block. Therefore, the major tasks of this dissertation are 1) performance-robust analog BIST circuit design and 2) test procedure development. Analog BIST circuits in this work consist of only low-accuracy analog components, which are usually easy to design and cost effective. The precision is then obtained by applying the so-called deterministic dynamic element matching technique to the low-accuracy analog cells. The test procedure and data processing designed for the BIST system are simple and can be implemented by small logic circuits. In this dissertation, we discuss the proposed BIST solutions to ADC and DAC linearity testing in chapter 3 and chapter 5, respectively. In each case, the structure of the test system, the test procedure, and the theoretical analysis of the test performance are presented. Simulation results are shown to verify the efficacy of the methods. The ADC BIST system is also verified experimentally. In addition, chapter 4 introduces a system-identification based reduced-code testing method for pipeline ADCs. This method is able to reduce test time by more than 95%. And it is compatible with the proposed BIST method discussed in chapter 3

    On-Chip Analog Circuit Design Using Built-In Self-Test and an Integrated Multi-Dimensional Optimization Platform

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    Nowadays, the rapid development of system-on-chip (SoC) market introduces tremendous complexity into the integrated circuit (IC) design. Meanwhile, the IC fabrication process is scaling down to allow higher density of integration but makes the chips more sensitive to the process-voltage-temperature (PVT) variations. A successful IC product not only imposes great pressure on the IC designers, who have to handle wider variations and enforce more design margins, but also challenges the test procedure, leading to more check points and longer test time. To relax the designers’ burden and reduce the cost of testing, it is valuable to make the IC chips able to test and tune itself to some extent. In this dissertation, a fully integrated in-situ design validation and optimization (VO) hardware for analog circuits is proposed. It implements in-situ built-in self-test (BIST) techniques for analog circuits. Based on the data collected from BIST, the error between the measured and the desired performance of the target circuit is evaluated using a cost function. A digital multi-dimensional optimization engine is implemented to adaptively adjust the analog circuit parameters, seeking the minimum value of the cost function and achieving the desired performance. To verify this concept, study cases of a 2nd/4th active-RC band-pass filter (BPF) and a 2nd order Gm-C BPF, as well as all BIST and optimization blocks, are adopted on-chip. Apart from the VO system, several improved BIST techniques are also proposed in this dissertation. A single-tone sinusoidal waveform generator based on a finite-impulse-response (FIR) architecture, which utilizes an optimization algorithm to enhance its spur free dynamic range (SFDR), is proposed. It achieves an SFDR of 59 to 70 dBc from 150 to 850 MHz after the optimization procedure. A low-distortion current-steering two-tone sinusoidal signal synthesizer based on a mixing-FIR architecture is also proposed. The two-tone synthesizer extends the FIR architecture to two stages and implements an up-conversion mixer to generate the two tones, achieving better than -68 dBc IM3 below 480 MHz LO frequency without calibration. Moreover, an on-chip RF receiver linearity BIST methodology for continuous and discrete-time hybrid baseband chain is proposed. The proposed receiver chain implements a charge-domain FIR filter to notch the two excitation signals but expose the third order intermodulation (IM3) tones. It simplifies the linearity measurement procedure–using a power detector is enough to analyze the receiver’s linearity. Finally, a low cost fully digital built-in analog tester for linear-time-invariant (LTI) analog blocks is proposed. It adopts a time-to-digital converter (TDC) to measure the delays corresponded to a ramp excitation signal and is able to estimate the pole or zero locations of a low-pass LTI system

    A Methodology for Implementing RF BiSTs in Production Testing to Replace RF Conventional Tests

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    Production testing of Radio Frequency (RF) devices is challenging due to the complex nature of the tests that have to be performed to verify functionality. In this dissertation a methodology to replace the complex and expensive RF functional tests with defect-oriented Built-in Self Tests (BiSTs) is detailed. If a design has sufficient margin to RF specifications then RF tests can be replaced with structural tests using a new data analysis technique called quadrant analysis, which is presented. Data from the analysis of over one million production units of said System on Chip (SoC) is presented along with the results of the analysis. The BiST techniques that have been used are discussed and a Texas Instruments 65 nm RF SoC with a Bluetooth and a FM core was used as a case study. The defect models that were used to develop the BiSTs are discussed as well. The scenario in which a design does not have sufficient margin to specification is also discussed. The data analysis method required in such a case is a regression analysis and the data from such an analysis is shown. The results prove that it is possible to replace expensive RF conventional tests with structural tests and that modern RFCMOS process technology and advances in design like the Digital Radio Processor (DRPTM) technology enable this. The Defective Parts Per Million (DPPM) impact of making this replacement is 27 units and is acceptable for RFCMOS high volume products. Finally, data showing test cost reduction of about 38% that resulted from the elimination of RF conventional tests is presented
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