2,349 research outputs found

    Electric prototype power processor for a 30cm ion thruster

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    An electrical prototype power processor unit was designed, fabricated and tested with a 30 cm mercury ion engine for primary space propulsion. The power processor unit used the thyristor series resonant inverter as the basic power stage for the high power beam and discharge supplies. A transistorized series resonant inverter processed the remaining power for the low power outputs. The power processor included a digital interface unit to process all input commands and internal telemetry signals so that electric propulsion systems could be operated with a central computer system. The electrical prototype unit included design improvement in the power components such as thyristors, transistors, filters and resonant capacitors, and power transformers and inductors in order to reduce component weight, to minimize losses, and to control the component temperature rise. A design analysis for the electrical prototype is also presented on the component weight, losses, part count and reliability estimate. The electrical prototype was tested in a thermal vacuum environment. Integration tests were performed with a 30 cm ion engine and demonstrated operational compatibility. Electromagnetic interference data was also recorded on the design to provide information for spacecraft integration

    All Social Media Is Not Created Equal: Instagram, Finsta, and Loneliness

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    Research on the relationships between social media use and loneliness has produced mixed findings, in part because people use social media in different ways. Finsta is a private Instagram account followed only by a small group of the user’s friends and is considered to be a more authentic form of social media. The purpose of the present study was to examine the differential associations of Instagram and Finsta use with social and emotional loneliness and to investigate off-line engagement as a potential mediator of these associations. With data from an online survey given to N = 330 emerging adults, a series of hierarchical linear regressions showed that Instagram use negatively predicted and Finsta use positively predicted social loneliness, whereas neither were associated with emotional loneliness. Furthermore, whereas Finsta use was not associated with off-line social engagement with friends (OSE-friend), Instagram use was positively associated with this variable. In addition, results showed that off-line social support with friends partially mediated the relationship between Instagram use and social loneliness. The findings imply that all social media are not created equal; even within the same platform (Instagram), differential associations were found with social loneliness depending on the type of account used

    The War Ministry of Winston Churchill

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    Reactor Simulator Testing

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    As part of the Nuclear Systems Office Fission Surface Power Technology Demonstration Unit (TDU) project, a reactor simulator test loop (RxSim) was design & built to perform integrated testing of the TDU components. In particular, the objectives of RxSim testing was to verify the operation of the core simulator, the instrumentation and control system, and the ground support gas and vacuum test equipment. In addition, it was decided to include a thermal test of a cold trap purification design and a pump performance test at pump voltages up to 150 V since the targeted mass flow rate of 1.75 kg/s was not obtained in the RxSim at the originally constrained voltage of 120 V. This paper summarizes RxSim testing. The gas and vacuum ground support test equipment performed effectively in NaK fill, loop pressurization, and NaK drain operations. The instrumentation and control system effectively controlled loop temperature and flow rates or pump voltage to targeted settings. The cold trap design was able to obtain the targeted cold temperature of 480 K. An outlet temperature of 636 K was obtained which was lower than the predicted 750 K but 156 K higher than the cold temperature indicating the design provided some heat regeneration. The annular linear induction pump (ALIP) tested was able to produce a maximum flow rate of 1.53 kg/s at 800 K when operated at 150 V and 53 Hz. Keywords: fission, space power, nuclear, liquid metal, NaK

    Beyond deficit-based models of learners' cognition: Interpreting engineering students' difficulties with sense-making in terms of fine-grained epistemological and conceptual dynamics

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    Researchers have argued against deficit-based explanations of students' troubles with mathematical sense-making, pointing instead to factors such as epistemology: students' beliefs about knowledge and learning can hinder them from activating and integrating productive knowledge they have. In this case study of an engineering major solving problems (about content from his introductory physics course) during a clinical interview, we show that "Jim" has all the mathematical and conceptual knowledge he would need to solve a hydrostatic pressure problem that we posed to him. But he reaches and sticks with an incorrect answer that violates common sense. We argue that his lack of mathematical sense-making-specifically, translating and reconciling between mathematical and everyday/common-sense reasoning-stems in part from his epistemological views, i.e., his views about the nature of knowledge and learning. He regards mathematical equations as much more trustworthy than everyday reasoning, and he does not view mathematical equations as expressing meaning that tractably connects to common sense. For these reasons, he does not view reconciling between common sense and mathematical formalism as either necessary or plausible to accomplish. We, however, avoid a potential "deficit trap"-substituting an epistemological deficit for a concepts/skills deficit-by incorporating multiple, context-dependent epistemological stances into Jim's cognitive dynamics. We argue that Jim's epistemological stance contains productive seeds that instructors could build upon to support Jim's mathematical sense-making: He does see common-sense as connected to formalism (though not always tractably so) and in some circumstances this connection is both salient and valued.Comment: Submitted to the Journal of Engineering Educatio

    Extended performance electric propulsion power processor design study. Volume 2: Technical summary

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    Electric propulsion power processor technology has processed during the past decade to the point that it is considered ready for application. Several power processor design concepts were evaluated and compared. Emphasis was placed on a 30 cm ion thruster power processor with a beam power rating supply of 2.2KW to 10KW for the main propulsion power stage. Extension in power processor performance were defined and were designed in sufficient detail to determine efficiency, component weight, part count, reliability and thermal control. A detail design was performed on a microprocessor as the thyristor power processor controller. A reliability analysis was performed to evaluate the effect of the control electronics redesign. Preliminary electrical design, mechanical design and thermal analysis were performed on a 6KW power transformer for the beam supply. Bi-Mod mechanical, structural and thermal control configurations were evaluated for the power processor and preliminary estimates of mechanical weight were determined

    Extended performance electric propulsion power processor design study. Volume 1: Executive summary

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    Several power processor design concepts were evaluated and compared. Emphasis was placed on a 30cm ion thruster power processor with a beam supply rating of 2.2kW to 10kW. Extensions in power processor performance were defined and were designed in sufficient detail to determine efficiency, component weight, part count, reliability and thermal control. Preliminary electrical design, mechanical design, and thermal analysis were performed on a 6kW power transformer for the beam supply. Bi-Mod mechanical, structural, and thermal control configurations were evaluated for the power processor, and preliminary estimates of mechanical weight were determined. A program development plan was formulated that outlines the work breakdown structure for the development, qualification and fabrication of the power processor flight hardware
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