29,147 research outputs found
NASA/Pratt and Whitney experimental clean combustor program: Engine test results
A two-stage vorbix (vortex burning and mixing) combustor and associated fuel system components were successfully tested in an experimental JT9D engine at steady-state and transient operating conditions, using ASTM Jet-A fuel. Full-scale JT9D experimental engine tests were conducted in a phase three aircraft experimental clean combustor program. The low-pollution combustor, fuel system, and fuel control concepts were derived from phase one and phase two programs in which several combustor concepts were evaluated, refined, and optimized in a component test rig. Significant pollution reductions were achieved with the combustor which meets the performance, operating, and installation requirements of the engine
Experimental clean combustor program, phase 3
A two-stage vortex burning and mixing combustor and associated fuel system components were successfully tested at steady state and transient operating conditions. The combustor exceeded the program goals for all three emissions species, with oxides of nitrogen 10 percent below the goal, carbon monoxide 26 percent below the goal, and total unburned hydrocarbons 75 percent below the goal. Relative to the JT9D-7 combustor, the oxides of nitrogen were reduced by 58 percent, carbon monoxide emissions were reduced by 69 percent, and total unburned hydrocarbons were reduced by 9 percent. The combustor efficiency and exit temperature profiles were comparable to those of production combustor. Acceleration and starting characteristics were deficient relative to the production engine
Evaluation of Federal Aviation Administration ion engine exhaust sampling rake
A FAA exhaust emissions rake was tested in the Experimental Clean Combustor Program, Phase 3 to permit comparison of the values of gaseous emissions and smoke measured by the FAA rake with those measured with the NASA Pratt and Whitney Aircraft (P and WA) rake used in the Phase 3 Experimental Clean Combustor Program and with station seven probes. The results showed that the levels of CO, THC, NOx and smoke measured by the FAA and NASA/P and WA rakes agree well at high power, but that CO emissions measured by the FAA rake were approximately 10 percent higher than those measured by the NASA/P and WA rake at low power
Hall effect encoding of brushless dc motors
Encoding mechanism integral to the motor and using the permanent magnets embedded in the rotor eliminates the need for external devices to encode information relating the position and velocity of the rotating member
Measurements of the absolute value of the penetration depth in high- superconductors using a tunnel diode resonator
A method is presented to measure the absolute value of the London penetration
depth, , from the frequency shift of a resonator. The technique
involves coating a high- superconductor (HTSC) with film of low - Tc
material of known thickness and penetration depth. The method is applied to
measure London penetration depth in YBa2Cu3O{7-\delta} (YBCO)
Bi2Sr2CaCu2O{8+\delta} (BSCCO) and Pr{1.85}Ce{0.15}CuO{4-\delta}\lambda (0)\lambda \approx 2790$ \AA, reported for the first
time.Comment: RevTex 4 (beta 4). 4 pages, 4 EPS figures. Submitted to Appl. Phys.
Let
c-Axis longitudinal magnetoresistance of the electron-doped superconductor Pr1.85Ce0.15CuO4
We report c-axis resistivity and longitudinal magnetoresistance measurements
of superconducting Pr1.85Ce0.15CuO4 single crystals. In the temperature range
13K<T<32K, a negative magnetoresistance is observed at fields just above Hc2.
Our studies suggest that this negative magnetoresistance is caused by
superconducting fluctuations. At lower temperatures (T<13K), a different
magnetoresistance behavior and a resistivity upturn are observed, whose origin
is still unknown.Comment: Accepted for publication in Phys. Rev.
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