8,204 research outputs found

    Acoustic and aerodynamic performance of a 1.83-meter (6-ft) diameter 1.25-pressure-ratio fan (QF-8)

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    A 1.25-pressure-ratio 1.83-meter (6-ft) tip diameter experimental fan stage with characteristics suitable for engine application on STOL aircraft was tested for acoustic and aerodynamic performance. The design incorporated proven features for low noise, including absence of inlet guide vanes, low rotor blade tip speed, low aerodynamic blade loading, and long axial spacing between the rotor and stator blade rows. The fan was operated with five exhaust nozzle areas. The stage noise levels generally increased with a decrease in nozzle area. Separation of the acoustic one-third octave results into broadband and pure-tone components showed the broadband noise to be greater than the corresponding pure-tone components. The sideline perceived noise was highest in the rear quadrants. The acoustic results of QF-8 were compared with those of two similar STOL application fans in the test series. The QF-8 had somewhat higher relative noise levels than those of the other two fans. The aerodynamic results of QF-8 and the other two fans were compared with corresponding results from 50.8-cm (20-in.) diam scale models of these fans and design values. Although the results for the full-scale and scale models of the other two fans were in reasonable agreement for each design, the full-scale fan QF-8 results showed poor performance compared with corresponding model results and design expectations. Facility effects of the full-scale fan QF-8 installation were considered in analyzing this discrepancy

    Low-frequency rear quadrant noise of a turbojet engine with exhaust duct muffling

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    A J-65 engine was run with a tuned sound-absorbing exhaust duct to study the internal and jet components of rear quadrant noise. Full muffler, hard wall duct, and regular production engine configurations were tested. The jet exhaust velocities were subsonic. The use of the exhaust muffler extended the relation between the jet noise and the eighth power of the jet velocity to lower velocities than for the hard wall duct

    Bidirectional fano algorithm for high throughput sequential decoding

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    Throughput improvement on bidirectional Fano algorithm

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    Estimating Sighting Proportions of American Alligator Nests during Helicopter Survey

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    Proportions of American alligator (Alligator mississippiensis) nests sighted during aerial survey in Florida were estimated based upon multiple surveys by different observers. We compared sighting proportions across habitats, nesting seasons, and observer experience levels. The mean sighting proportion across all habitats and years was 0.736 (SE=0.024). Survey counts corrected by the mean sighting proportion reliably predicted total nest counts (R2=0.933). Sighting proportions did not differ by habitat type (P=0.668) or year P=0.328). Experienced observers detected a greater proportion of nests (P<O.OOOl) than did either less experienced or inexperienced observers. Reliable estimates of nest abundance can be derived from aerial counts of alligator nests when corrected by the appropriate sighting proportion

    Acoustic and aerodynamic performance of a 1.5-pressure-ratio, 1.83-meter (6 ft) diameter fan stage for turbofan engines (QF-2)

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    The fan was externally driven by an electric motor. Design features for low-noise generation included the elimination of inlet guide vanes, long axial spacing between the rotor and stator blade rows, and the selection of blade-vane numbers to achieve duct-mode cutoff. The fan QF-2 results were compared with those of another full-scale fan having essentially identical aerodynamic design except for nozzle geometry and the direction of rotation. The fan QF-2 aerodynamic results were also compared with those obtained from a 50.8 cm rotor-tip-diameter model of the reverse rotation fan QF-2 design. Differences in nozzle geometry other than exit area significantly affected the comparison of the results of the full-scale fans

    Acoustic and aerodynamic performance of a 1.83 meter (6 foot) diameter 1.2 pressure ratio fan (QF-6)

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    A 1.2-pressure-ratio, 1.83-meter-(6-ft-) diameter experimental fan stage with characteristics suitable for use in STOL aircraft engines was tested for acoustic and aerodynamic performance. The design incorporated features for low noise, including absence of inlet guide vanes, low rotor-blade-tip speed, low aerodynamic blade loading, and long axial spacing between the rotor and stator rows. The stage was run with four nozzles of different area. The perceived noise along a 152.4 meter (500-ft) sideline was rear-quadrant dominated with a maximum design-point level of 103.9 PNdb. The acoustic 1/3-octave results were analytically separated into broadband and pure-tone components. It was found that the stage noise levels generally increase with a decrease in nozzle area, with this increase observed primarily in the broadband noise component. A stall condition was documented acoustically with a 90-percent-of-design-area nozzle

    The effects of long-day lighting and removal of young leaves on tomato yield

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    While low intensity long-day (LD) lighting has been shown to enhance the growth of young plants under low light levels, its effect on the yield of a long-season glasshouse tomato crop has not been previously examined. LD were provided by the use of tungsten lamps (2.8 μmol m-2 s-1 at approx. 0.5 m from the ground) between 04.00 h to sunrise and from sunset until 20.00 h (GMT). LD lighting increased leaf chlorophyll contents, and the numbers of flowers and fruits set per truss when the plants were young. However, this treatment did not affect the total yield of tomatoes. Different leaf removal treatments were applied within each glasshouse compartment. A previous experiment had shown that reducing the leaf area index (LAI) from 5.2 to 2.6, by removing old leaves, did not affect yield. It was also thought that removal of young leaves reduced the total vegetative sink-strength and favoured assimilate partitioning into the fruit. Therefore, removal of young leaves could increase fruit yield. In the present experiments, one-third of the leaves were removed in March (those immediately below each truss) and, subsequently, every third leaf was removed at an early stage of its development. This reduced the LAI from 4.1 to 2.9 and resulted in a loss of yield from 3 – 4 weeks after leaf removal until the end of the experiment, at which point there was an 8% loss of cumulative yield due to a reduction in the average number of fruits set per truss and in mean fruit weight. We postulate that the light which would have been intercepted by young photosynthetically-efficient leaves at the top of the canopy was intercepted instead by older leaves which were less efficient, reducing overall net canopy photosynthesis

    Acoustic and aerodynamic performance of a variable-pitch 1.83-meter-(6-ft) diameter 1.20-pressure-ratio fan stage (QF-9)

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    Far field noise data and related aerodynamic performance are presented for a variable pitch fan stage having characteristics suitable for low noise, STOL engine application. However, no acoustic suppression material was used in the flow passages. The fan was externally driven by an electric motor. Tests were made at several forward thrust rotor blade pitch angles and one for reverse thrust. Fan speed was varied from 60 to 120 percent of takeoff (design) speed, and exhaust nozzles having areas 92 to 105 percent of design were tested. The fan noise level was at a minimum at the design rotor blade pitch angles of 64 deg for takeoff thrust and at 57 deg for approach (50 percent takeoff thrust). Perceived noise along a 152.4-m sideline reached 100.1 PNdb for the takeoff (design) configuration for a stage pressure ratio of 1.17 and thrust of 57,600 N. For reverse thrust the PNL values were 4 to 5 PNdb above the takeoff values at comparable fan speeds

    Forward acoustic performance of a shock-swallowing high-tip-speed fan (QF-13)

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    Forward noise and overall aerodynamic performance data are presented for a high-tip-speed fan having rotor blade airfoils designed to alter the conventional leading-edge bow shocks to weak, oblique shocks which are swallowed within the interblade channels. It was anticipated that the swallowed shocks would minimize the generation of multiple-pure-tone noise. In the speed range where the shocks presumably were swallowed, the multiple-tone noise was lowered only about 3 decibels. Comparison with several high-speed fans on a thrust-corrected basis indicates that the present fan was the quietest in total forward noise at low speeds but offered no advantage at high speeds
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