189 research outputs found

    Effect of ratio of wall boundary layer thickness to jet diameter on mixing of a normal hydrogen jet in a supersonic stream

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    A preliminary experimental program was conducted to determine the effect of the ratio of the free-stream boundary-layer thickness to jet diameter on the secondary jet penetration and mixing rate. Tests were conducted on a flat plate in a Mach number 4.05 airflow with sonic injection of hydrogen normal to the free-stream direction from circular underexpanded injectors. The ratio of boundary-layer thickness to jet diameter ranged from 1.25 to 6.5. Previous correlations of mixing performance were modified to account for the effect of the ratio of boundary-layer thickness to jet diameter

    Normal injection of helium from swept struts into ducted supersonic flow

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    Recent design studies have shown that airframe-integrated scramjets should include instream mounted, swept-back strut fuel injectors to obtain short combustors. Because there was no data in the literature on mixing characteristics of swept strut fuel injectors, the present investigation was undertaken to provide such data. This investigation was made with two swept struts in a closed duct at Mach number of 4.4 and nominal jet-to-air mass flow ratio of 0.029 with helium used to simulate hydrogen fuel. The data is compared with flat plate mounted normal injector data to obtain the effect of swept struts on mixing. Three injector patterns were evaluated representing the range of hole spacing and jet-to-freestream dynamic pressure ratio of interest. Measured helium concentration, pitot pressure, and static pressure in the downstream mixing region are used to generate contour plots necessary to define the mixing region flow field and the mixing parameters

    Evaluation of a bulk calorimeter and heat balance for determination of supersonic combustor efficiency

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    Results are presented from the shakedown and evaluation test of a bulk calorimeter. The calorimeter is designed to quench the combustion at the exit of a direct-connect, hydrogen fueled, scramjet combustor model, and to provide the measurements necessary to perform an analysis of combustion efficiency. Results indicate that the calorimeter quenches reaction, that reasonable response times are obtained, and that the calculated combustion efficiency is repeatable within + or -3 percent and varies in a regular way with combustor model parameters such as injected fuel equivalence ratio

    Interaction between step fuel injectors on opposite walls in a supersonic combustor model

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    Results are presented from an experimental investigation of perpendicular, hydrogen fuel injection and combustion from opposing walls in a scramjet combustor model using a longitudinally staged laterally inline step-injection configuration. The model represents a portion of the flow in the Langley integrated modular scramjet engine combustor operating at a flight Mach number of 7. When operating at a ratio of jet pressure to free-stream dynamic pressure of 3, the injectors produce a bulk equivalence ratio of unity. This investigation represents part of a continuing study of the modular engine fuel injectors and is specifically designed to eliminate the adverse lateral pressure gradient observed at the injector location in a previous test. Flow survey contours at three axial locations, ranging from one-third of the engine combustor length to the total engine combustor length, are used to determine mixing efficiency and fuel distribution. Wall static pressures are analyzed by using one-dimensional theory to determine the combustion efficiency. Results show a significant improvement over previous injector designs tested in this duct geometry

    Criteria for self-ignition of supersonic hydrogen-air mixtures

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    A correlation of available self ignition data for supersonic hydrogen-air mixtures in configurations representative of scramjet combustors was made. The correlation was examined in light of simplified ignition-limit models. The data and model included cases of injection from transverse fuel jets on walls, transverse jets behind swept and unswept steps, and transverse injection ahead of swept and unswept steps and strut bases. The results provide useful guidance for predicting self ignition in a variety of applications. The likely regions for self ignition in a combustor are given in order of merit

    Nonreactive mixing study of a scramjet swept-strut fuel injector

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    The results are presented of a cold-mixing investigation performed to supply combustor design information and to determine optimum normal fuel-injector configurations for a general scramjet swept-strut fuel injector. The experimental investigation was made with two swept struts in a closed duct at a Mach number of 4.4 and a nominal ratio of jet mass flow to air mass flow of 0.0295, with helium used to simulate hydrogen fuel. Four injector patterns were evaluated; they represented the range of hole spacing and the ratio of jet dynamic pressure to free-stream dynamic pressure. Helium concentration, pitot pressure, and static pressure in the downstream mixing region were measured to generate the contour plots needed to define the mixing-region flow field and the mixing parameters. Experimental results show that the fuel penetration from the struts was less than the predicted values based on flat-plate data; but the mixing rate was faster and produced a mixing length less than one-half that predicted

    The NASA Hyper-X Program

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    This paper provides an overview of NASA's Hyper-X Program; a focused hypersonic technology effort designed to move hypersonic, airbreathing vehicle technology from the laboratory environment to the flight environment. This paper presents an overview of the flight test program, research objectives, approach, schedule and status. Substantial experimental database and concept validation have been completed. The program is currently concentrating on the first, Mach 7, vehicle development, verification and validation in preparation for wind-tunnel testing in 1998 and flight testing in 1999. Parallel to this effort the Mach 5 and 10 vehicle designs are being finalized. Detailed analytical and experimental evaluation of the Mach 7 vehicle at the flight conditions is nearing completion, and will provide a database for validation of design methods once flight test data are available

    Targeted nanopore sequencing enables complete characterisation of structural deletions initially identified using exon-based short-read sequencing strategies

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    Background The widespread adoption of exome sequencing has greatly increased the rate of genetic diagnosis for inherited conditions. However, the detection and validation of large deletions remains challenging. While numerous bioinformatics approaches have been developed to detect deletions from whole - exome sequencing and targeted panels, further work is typically required to define the physical breakpoints or integration sites. Accurate characterisation requires either expensive follow - up whole - genome sequencing or the time - consuming, laborious process of PCR walking, both of which are challenging when dealing with the repeat sequences which frequently intersect deletion breakpoints. The aim of this study was to develop a cost-effective, long-range sequencing method to characterise deletions. Methods Genomic DNA was amplified with primers spanning the deletion using long-range PCR and the products purified. Sequencing was performed on MinION flongle flowcells. The resulting fast5 files were basecalled using Guppy, trimmed using Porechop and aligned using Minimap2. Filtering was performed using NanoFilt. Nanopore sequencing results were verified by Sanger sequencing. Results Four cases with deletions detected following comparative read-depth analysis of targeted short-read sequencing were analysed. Nanopore sequencing defined breakpoints at the molecular level in all cases including homozygous breakpoints in EYS, CNGA1 and CNGB1 and a heterozygous deletion in PRPF31. All breakpoints were verified by Sanger sequencing. Conclusions In this study, a quick, accurate and cost - effective method is described to characterise deletions identified from exome, and similar data, using nanopore sequencing

    Three-component force measurements on a large scramjet in a shock tunnel

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    A stress-wave force balance for measurement of thrust, lift, and pitching moment on a large scramjet model (40 kg in mass, 1.165 in in length) in a reflected shock tunnel has been designed, calibrated, and tested. Transient finite element analysis was used to model the performance of the balance. This modeling indicates that good decoupling of signals and low sensitivity of the balance to the distribution of. the load can be achieved with a three-bar balance. The balance was constructed and calibrated by applying a series of point loads to the model. A good comparison between finite element analysis and experimental results was obtained with finite element analysis aiding in the interpretation of some experimental results. Force measurements were made in a shock tunnel both with and without fuel injection, and measurements were compared with predictions using simple models of the scramjet and combustion. Results indicate that the balance is capable of resolving lift, thrust, and pitching moments with and without combustion. However vibrations associated with tunnel operation interfered with the signals indicating the importance of vibration isolation for accurate measurements
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