3,332 research outputs found

    The Trial of Andrew Johnson 1868

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    Jesus as interceding high priest and sacrifice in Hebrews : a response to Nicholas Moore

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    Is Jesus’ perpetual intercession for his people in Hebrews (Heb. 7.25) understood as a constitutive part of his atoning, high-priestly ministry? Nicholas Moore argues that Jesus’ act of sitting at God’s right hand is the decisive end of Jesus’ atoning sacrifice and so also of Hebrews’ Yom Kippur analogy. Among other points, I argue in response that Jesus’ ongoing absence from his people, status as high priest and current location in the heavenly holy of holies imply that Hebrews’ Yom Kippur analogy extends beyond Jesus’ act of sitting to include his present ministry of intercession. Not only were prayer and atoning sacrifice closely correlated for Second Temple Jews, Hebrews presents Jesus as the high priest who, in his resurrected humanity, is always also the sacrifice in the Father’s presence. Jesus presented himself to the Father once, but he is perpetually the high priest and sacrifice who ministers in God’s presence. For Hebrews, the Yom Kippur analogy (and so also Jesus’ atoning ministry) ends when, like the earthly high priests, Jesus leaves the heavenly holy of holies to return to and again be present with his people (Heb. 9.28). Only then will his followers receive the salvation for which they are waiting. Until that approaching day arrives, Jesus’ ongoing intercession with his Father ensures that his people will be saved completely.Publisher PDFNon peer reviewe

    Day of Atonement

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    Atonement

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    Cold-air investigation of a 4 1/2 stage turbine with stage-loading factor of 4.66 and high specific work output. 2: Stage group performance

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    The stage group performance of a 4 1/2 stage turbine with an average stage loading factor of 4.66 and high specific work output was determined in cold air at design equivalent speed. The four stage turbine configuration produced design equivalent work output with an efficiency of 0.856; a barely discernible difference from the 0.855 obtained for the complete 4 1/2 stage turbine in a previous investigation. The turbine was designed and the procedure embodied the following design features: (1) controlled vortex flow, (2) tailored radial work distribution, and (3) control of the location of the boundary-layer transition point on the airfoil suction surface. The efficiency forecast for the 4 1/2 stage turbine was 0.886, and the value predicted using a reference method was 0.862. The stage group performance results were used to determine the individual stage efficiencies for the condition at which design 4 1/2 stage work output was obtained. The efficiencies of stages one and four were about 0.020 lower than the predicted value, that of stage two was 0.014 lower, and that of stage three was about equal to the predicted value. Thus all the stages operated reasonably close to their expected performance levels, and the overall (4 1/2 stage) performance was not degraded by any particularly inefficient component

    Cold air investigation of 4 1/2-stage turbine with stage loading factor of 4.66 and high specific work output. 1: Overall performance

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    The turbine developed design specific work output at design speed at a total pressure ratio of 6.745 with a corresponding efficiency of 0.855. The efficiency (0.855)was 3.1 points lower than the estimated efficiency quoted by the contractor in the design report and 0.7 of a point lower than that determined by a reference prediction method. The performance of the turbine, which was a forced vortex design, agreed with the performance determined by the prediction method to about the same extent as did the performance of three reference high stage loading factor turbines, which were free vortex designs
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