264 research outputs found

    Component Performance Investigation of J71 Experimental Turbine I : Over-all Performance with 97-percent-design Stator Areas

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    The over-all component performance characteristics of a J71 experimental three-stage turbine with 97 percent design stator areas were determined over a range of speed and pressure ratio at inlet-air conditions of approximately 35 inches of mercury absolute and 700 degrees R. The turbine break internal efficiency at design operating conditions was 0.877; the maximum efficiency of 0.886 occurred at a pressure ratio of 4.0 at 120 percent of design equivalent rotor speed. In general, the turbine yielded a wide range of efficient operation, permitting flexibility in the choice of different modes of engine operation. Limiting blade loading of the third rotor was approached but not obtained over the range of conditions investigated herein. At the design operating point, the turbine equivalent weight flow was approximately 105 percent of design. Choking of the third-rotor blades occurred at design speed and an over-all pressure ratio of 4.2

    Component Performance Investigation of J71 Type II Turbines: III - Overall Performance of J71 Type IIA Turbine

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    The over-all component performance characteristics of the J71 Type IIA three-stage turbine were experimentally determined over a range of speed and over-all turbine total-pressure ratio at inlet-air conditions af 35 inches of mercury absolute and 700 deg. R. The results are compared with those obtained for the J71 Type IIF turbine, which was previously investigated, the two turbines being designed for the same engine application. Geometrically the two turbines were much alike, having the same variation of annular flow area and the same number of blades for corresponding stator and rotor rows. However, the blade throat areas downstream of the first stator of the IIA turbine were smaller than those of the IIF; and the IIA blade profiles were curve-backed, whereas those of the IIF were straight-backed. The IIA turbine passed the equivalent design weight flow and had a brake internal efficiency of 0.880 at design equivalent speed and work output. A maximum efficiency of 0.896 occurred at 130 percent of design equivalent speed and a pressure ratio of 4.0. The turbine had a wide range of efficient operation. The IIA turbine had slightly higher efficiencies than the IIF turbine at comparable operating conditions. The fact that the IIA turbine obtained the design equivalent weight flow at the design equivalent operating point was probably a result of the decrease in the blading throat areas downstream of the first stator from those of the IIF turbine, which passed 105 percent of design weight flow at the corresponding operating point. The third stator row of blades of the IIA turbine choked at the design equivalent speed and at an over-all pressure ratio of 4.2; the third rotor choked at a pressure ratio of approximately 4.

    Component Performance Investigation of J71 Experimental Turbine VII: Effect of First-stator Adjustment; Over-all Performance of J71-97 Turbine with 87-percent-design Stator Area

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    The performance results, as well as a compressor-turbine match point study based on a particular mode of engine operation, are compared with those previously obtained with the same turbine having first-stator areas 70, 95.6, and 132 percent of design. Maximum efficiencies for all turbine configurations were high, on the order of 87 to 89 percent. The efficiencies obtained at the match points for the 87-, 95.6-, and 132-percent turbines were slightly lower. No match point for the 70-percent turbine was obtained because, with first-stator areas less than 75.5 percent of design, the turbine would develop insufficient work to drive the compressor at the match point
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