5 research outputs found

    Space Shuttle Columbia Post-Accident Analysis and Investigation

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    Although the loss of the Space Shuttle Columbia and its crew was tragic, the circumstances offered a unique opportunity to examine a multitude of components which had experienced one of the harshest environments ever encountered by engineered materials: a break up at a velocity in excess of Mach 18 and an altitude exceeding 200,000 feet (63 KM), resulting in a debris field 645 miles/l,038 KM long and 10 miles/16 KM wide. Various analytical tools were employed to ascertain the sequence of events leading to the disintegration of the Orbiter and to characterize the features of the debris. The testing and analyses all indicated that a breach in a left wing reinforced carbon/carbon composite leading edge panel was the access point for hot gasses generated during re-entry to penetrate the structure of the vehicle and compromise the integrity of the materials and components in that area of the Shuttle. The analytical and elemental testing utilized such techniques as X-Ray Diffraction (XRD), Energy Dispersive X-Ray (EDX) dot mapping, Electron Micro Probe Analysis (EMPA), and X-Ray Photoelectron Spectroscopy (XPS) to characterize the deposition of intermetallics adjacent to the suspected location of the plasma breach in the leading edge of the left wing, Fig. 1

    The Space Shuttle Columbia Accident Investigation and Reconstruction: Two Years Later

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    The Space Shuttle Columbia was lost during re-entry over two years ago. Since the release of the official materials-related findings in August of 2003, additional testing and analysis of select pieces of debris has continued. Microanalytical techniques, including EMPA, ESCA, and x-ray elemental dot mapping, were employed during the initial investigation; the results related the microstructural characteristics of deposit layers to the breach location in the leading edge of the left wing. Such characteristics included deposition order, composition, and distribution. Subsequent to the original efforts, new analytical data and information, not available at the time of the primary investigation, has been generated. This data was obtained via a low-vacuum SEM, fitted not only with a light-element EDS detector, but an XRF tube as well. Essentially, for elements up to sodium, classic EDS was utilized; above sodium, XRF was used. Predominantly, the elements of interest were aluminum, titanium, chromium, iron, nickel, and copper. The findings of both old and new data are compared, and their application to the overall accident investigation detailed

    Materials Analysis: A Key to Unlocking the Mystery of the Columbia Tragedy

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    Materials analyses of key forensic evidence helped unlock the mystery of the loss of space shuttle Columbia that disintegrated February 1, 2003 while returning from a 16-day research mission. Following an intensive four-month recovery effort by federal, state, and local emergency management and law officials, Columbia debris was collected, catalogued, and reassembled at the Kennedy Space Center. Engineers and scientists from the Materials and Processes (M&P) team formed by NASA supported Columbia reconstruction efforts, provided factual data through analysis, and conducted experiments to validate the root cause of the accident. Fracture surfaces and thermal effects of selected airframe debris were assessed, and process flows for both nondestructive and destructive sampling and evaluation of debris were developed. The team also assessed left hand (LH) airframe components that were believed to be associated with a structural breach of Columbia. Analytical data collected by the M&P team showed that a significant thermal event occurred at the left wing leading edge in the proximity of LH reinforced carbon carbon (RCC) panels 8 and 9. The analysis also showed exposure to temperatures in excess of 1,649 C, which would severely degrade the support structure, tiles, and RCC panel materials. The integrated failure analysis of wing leading edge debris and deposits strongly supported the hypothesis that a breach occurred at LH RCC panel 8
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