3 research outputs found

    Effects of acoustic sources

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    An experiment was conducted to determine the effect of acoustics on the laminar flow on the side of a nacelle. A flight test was designed to meet this goal and a brief review of the purpose is given. A nacelle with a significant length of laminar flow was mounted on the wing of NASA OV-1. Two noise sources are also mounted on the wing: one in the center body of the nacelle; the second in a wing mounted pod outboard of the nacelle. These two noise sources allow for a limited study of the effect of source direction in addition to control of the acoustic level and frequency. To determine the range of Tollmien-Schlichting frequencies, a stability analysis using the pressure coefficient distribution along the side of the nacelle was performed. Then by applying these frequencies and varying the acoustic level, a study of the receptivity of the boundary layer to the acoustic signal, as determined by the shortening of the length of laminar flow, was conducted. Results are briefly discussed

    Status report on a natural laminar-flow nacelle flight experiment

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    The natural laminar flow (NLF) nacelle experiment is part of a drag reduction production program, and has the dual objectives of studying the extent of NLF on full scale nacelles in a flight environment and the effect of acoustic disturbance on the location of transition on the nacelle surface. The experiment is being conducted in two phases: (1) an NLF fairing was flown on a full scale Citation nacelle to develop the experiment technique and establish feasibility; (2) full scale, flow through, NLF nacelles located below the right wing of an experimental NASA OV-1 aircraft are evaluated. The measurements of most interest are the static pressure distribution and transition location on the nacelle surface, and the fluctuating pressure levels associated with the noise sources. Data are collected in combinations of acoustic frequencies and sound pressure levels. The results of phase 2 tests to date indicate that on shape GE2, natural laminar flow was maintained as far aft as the afterbody joint at 50 percent of the nacelle length. An aft facing step at this joint caused premature transition at this station. No change was observed in the transition pattern when the noise sources were operated
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