3,240 research outputs found

    Acoustic and aerodynamic performance investigation of inverted velocity profile coannular plug nozzles, comprehensive data report, volume 2

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    Volume 2 of a three volume report is presented. Volume 2 presents acoustic data comparisons in graphic form

    Acoustic and aerodynamic performance investigation of inverted velocity profile coannular plug nozzles

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    The results of model scale parametric static and wind tunnel aerodynamic performance tests on unsuppressed coannular plug nozzle configurations with inverted velocity profile are discussed. The nozzle configurations are high-radius-ratio coannular plug nozzles applicable to dual-stream exhaust systems typical of a variable cycle engine for Advanced Supersonic Transport application. In all, seven acoustic models and eight aerodynamic performance models were tested. The nozzle geometric variables included outer stream radius ratio, inner stream to outer stream ratio, and inner stream plug shape. When compared to a conical nozzle at the same specific thrust, the results of the static acoustic tests with the coannular nozzles showed noise reductions of up to 7 PNdB. Extensive data analysis showed that the overall acoustic results can be well correlated using the mixed stream velocity and the mixed stream density. Results also showed that suppression levels are geometry and flow regulation dependent with the outer stream radius ratio, inner stream-to-outer stream velocity ratio and inner stream velocity ratio and inner stream plug shape, as the primary suppression parameters. In addition, high-radius ratio coannular plug nozzles were found to yield shock associated noise level reductions relative to a conical nozzle. The wind tunnel aerodynamic tests showed that static and simulated flight thrust coefficient at typical takeoff conditions are quite good - up to 0.98 at static conditions and 0.974 at a takeoff Mach number of 0.36. At low inner stream flow conditions significant thrust loss was observed. Using an inner stream conical plug resulted in 1% to 2% higher performance levels than nozzle geometries using a bent inner plug

    Beating heart coronary surgery and renal function: a prospective randomised study (Presented at 18th Spring Meeting of the Association of Cardiothoracic Anaesthetists: Selected abstracts, Cambridge, UK. 22 June 2001)

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    Introduction Cardiopulmonary bypass (CPB) is widely regarded as an important contributor to renal failure, a well recognised complication, following coronary artery surgery (CABG). Off-pump coronary surgery (OPCAB) is intuitively considered renoprotective. We examine the extent of renal glomerular and tubular injury in low-risk patients undergoing either OPCAB or on-pump coronary artery bypass (ONCAB).Methods Forty patients awaiting elective CABG were prospectively randomized into those undergoing OPCAB (n = 20) and ONCAB (n = 20). Table 1 illustrates the exclusion criteria. Glomerular and tubular injury were assessed, respectively, by urinary excretion of microalbumin and retinol binding protein (RBP) indexed to urinary creatinine [1]. Daily measurements were made from admission to postoperative day 5. Fluid balance, serum creati-nine and blood urea were also monitored. Results No mortality or renal complication was observed. Both groups had similar demographic make-up. The OPCAB group received fewer coronary grafts than their counterparts (1.8 versus 2.8; P = 0.002). Serum creatinine and blood urea remained normal in both groups throughout the study. A dramatic and similar rise in mean ± 2SD urinary RBP:creatinine ratio occurred in both groups peaking on day 1 (3183 ± 2534 versus 4035 ± 4078; P = 0.43) before returning to baseline levels. These trends were also observed with the urinary microalbumin:creatinine ratio (5.05 ± 2.66 versus 6.77 ± 5.76; P = 0.22). ONCAB patients had a significantly more negative fluid balance on postoperative day 2 (-183 ± 1118 versus 637 ± 847 ml; P < 0.05). Conclusions Although renal dysfunction did not clinically occur in any patient, sensitive indicators revealed significant and similar injury to both renal tubules and glomeruli following either OPCAB or ONCAB. These suggest that avoidance of CPB per se does not offer additional renoprotection to patients at low risk of perioperative renal insult during CABG

    Free-jet investigation of mechanically suppressed, high radius ratio coannular plug model nozzles

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    The experimental and analytical acoustic results of a scale-model investigation or unsuppressed and mechanically suppressed high-radius ratio coannular plug nozzles with inverted velocity and temperature profiles are summarized. Nine coannular nozzle configurations along with a reference conical nozzle were evaluated in the Anechoic Free-Jet Facility for a total of 212 acoustic test points. Most of the tests were conducted at variable cycle engine conditions applicable to advanced high speed aircraft. The tested nozzles included coannular plug nozzles with both convergent and convergent-divergent (C-D) terminations in order to evaluate C-D effectiveness in the reduction of shock-cell noise and 20 and 40 shallow-chute mechanical suppressors in the outer stream in order to evaluate their effectiveness in the reduction of jet noise. In addition to the acoustic tests, mean and turbulent velocity measurements were made on selected plumes of the 20 shallow-chute configuration using a laser velocimeter. At a mixed jet velocity of 700 m/sec, the 20 shallow-chute suppressor configuration yielded peak aft quadrant suppression of 11.5 and 9 PNdB and forward quadrant suppression of 7 and 6 PNdB relative to a baseline conical nozzles during static and simulated flight, respectively. The C-D terminations were observed to reduce shock-cell noise. An engineering spectral prediction method was formulated for mechanically suppressed coannular plug nozzles

    A review of recent activities in the NASA CELSS program

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    A CELSS (Controlled Ecological Life Support System) is a device that utilizes photosynthetic organisms and light energy to regenerate waste materials into oxygen and food for a crew in space. The results of studies with the CELSS program suggest that a bioregenerative life support system is a useful and effective method of regenerating consumable materials for crew sustenance. The data suggests that the operation of a CELSS in space is practical if plants can be made to behave predictably in the space environment. Much of the work centers on the biological components of the CELSS system. Ways of achieving high efficiency and long term stability of all components of the system are examined. Included are explorations of the conversion of nonedible cellulose to edible materials, nitrogen fixation by biological and chemical methods, and methods of waste processing. A description is provided of the extent to which a bioregenerative life support system can meet the constraints of the space environment, and the degree is assessed to which system efficiency and stability can be increased during the next decade

    Engineering verification of the biomass production chamber

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    The requirements for life support systems, both biological and physical-chemical, for long-term human attended space missions are under serious study throughout NASA. The KSC 'breadboard' project has focused on biomass production using higher plants for atmospheric regeneration and food production in a special biomass production chamber. This chamber is designed to provide information on food crop growth rate, contaminants in the chamber that alter plant growth requirements for atmospheric regeneration, carbon dioxide consumption, oxygen production, and water utilization. The shape and size, mass, and energy requirements in relation to the overall integrity of the biomass production chamber are under constant study

    Effects of atmospheric CO2 on photosynthetic characteristics of soybean leaves

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    Soybean (Glycine max. cv. McCall) plants were grown at 500, 1000, and 2000 umol mol (exp -1) CO2 for 35 days with a photosynthetic photon flux of 300 umol m (exp -2) s (-1). Individual leaves were exposed to step changes of photosynthetic photon flux to study CO2 assimilation rates (CAR), i.e., leaf net photosynthesis. In general, CAR increased when CO2 increased from 500 to 1000 umol mol (exp -1), but not from 1000 to 2000 umol mol (exp -1). Regardless of the CO2 level, all leaves showed similar CAR at similar CO2 and PPF. This observation contrasts with reports that plants tend to become 'lazy' at elevated CO2 levels over time. Although leaf stomatal conductance (to water vapor) showed diurnal rhythms entrained to the photoperiod, leaf CAR did not show these rhythms and remained constant across the light period, indicating that stomatal conductance had little effect on CAR. Such measurements suggest that short-term changes in CO2 exchange dynamics for a controlled ecological life support system can be closely predicted for an actively growing soybean crop

    VCE early acoustic test results of General Electric's high-radius ratio coannular plug nozzle

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    Results of variable cycle engine (VCE) early acoustic engine and model scale tests are presented. A summary of an extensive series of far field acoustic, advanced acoustic, and exhaust plume velocity measurements with a laser velocimeter of inverted velocity and temperature profile, high radius ratio coannular plug nozzles on a YJ101 VCE static engine test vehicle are reviewed. Select model scale simulated flight acoustic measurements for an unsuppressed and a mechanical suppressed coannular plug nozzle are also discussed. The engine acoustic nozzle tests verify previous model scale noise reduction measurements. The engine measurements show 4 to 6 PNdB aft quadrant jet noise reduction and up to 7 PNdB forward quadrant shock noise reduction relative to a fully mixed conical nozzle at the same specific thrust and mixed pressure ratio. The influences of outer nozzle radius ratio, inner stream velocity ratio, and area ratio are discussed. Also, laser velocimeter measurements of mean velocity and turbulent velocity of the YJ101 engine are illustrated. Select model scale static and simulated flight acoustic measurements are shown which corroborate that coannular suppression is maintained in forward speed
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