To the process of production, it was not uncommon products that towel produced having the quality of being not as expected and became a waste activities. Research aims to identify problems with the quality and get the repair proposal reach failure zero (zero defect) By using lean six sigma analysis DMAIC (Define, Measure, Analyze, Improved, Control). The results of the study, in phase define the results of the questionnaire waste workshop. Then the total phase measure shows that the level of sigma a towel CV.Ngremboko 3,461835 σas much as.This figure does not having the capacity of the process by which good so they should is continuously repaired. The next stage of the point of view of a diagram pareto analyze phase in a can defect highest overall performance is a towel dirty at 19,72% and thread not 15,60% are woven as much as. As for the results of the analysis using Fishbone Diagram used looking for the factors causing the defect and an analysis of why the 5 or root cause of each the human factor, a method of, the environment and the engine has done next cause of the proposed fixes at phase improved to reduce problems that emerged with the methods 5R. And the final phase of the namely phase control carried out as an effort to standardization which was expanded using procedure used as standard work guidelines so that phase control becomes an activity enjoyed both cultural practices systematic who work in its implementation in lean or on a continual