Combustion and NOx emission characteristics of a retrofitted down-fired 660 MWe utility boiler at different loads

Abstract

Industrial experiments were performed for a retrofitted 660 MWe full-scale down-fired boiler. Measurements of ignition of the primary air/fuel mixture flow, the gas temperature distribution of the furnace and the gas components in the furnace were conducted at loads of 660, 550 and 330 MWe. With decreasing load, the gas temperature decreases and the ignition position of the primary coal/air flow becomes farther along the axis of the fuel-rich pipe in the burner region under the arches. The furnace temperature also decreases with decreasing load, as does the difference between the temperatures in the burning region and the lower position of the burnout region. With decreasing load, the exhaust gas temperature decreases from 129.8 °C to 114.3 °C, while NOx emissions decrease from 2448 to 1610 mg/m3. All three loads result in low carbon content in fly ash and great boiler thermal efficiency higher than 92%. Compared with the case of 660 MWe before retrofit, the exhaust gas temperature decreased from 136 to 129.8 °C, the carbon content in the fly ash decreased from 9.55% to 2.43% and the boiler efficiency increased from 84.54% to 93.66%.Down-fired boiler Retrofit Carbon content in fly ash Thermal efficiency

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    Last time updated on 06/07/2012