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Results of TC-1 boost pump icing tests in the space power facility

Abstract

A series of tests were conducted in the space power facility to investigate the failure of the Centaur oxidizer boost pump during the Titan/Centaur proof flight February 11, 1974. The three basic objectives of the tests were: (1) demonstrate if an evaporative freezing type failure mechanism could have prevented the pump from operating, (2) determine if steam from the exhaust of one of the attitude control engine could have entered a pump seal cavity and caused the failure, and (3) obtain data on the heating effects of the exhaust plume from a hydrogen peroxide attitude control engine

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