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Evaluation of ball and roller bearings restored by grinding

Abstract

The restoration by grinding of those rolling element bearings which are currently being discarded at aircaft engine and transmission overhaul is considered. Three bearing types were selected from the UH-1 helicopter engine and transmission for the pilot program. Groups of each of these bearings were visually and dimensionally inspected for suitability for restoration. A total of 250 bearings were restored by grinding. Of this number, 30 bearings from each type were endurance tested to a TBO of 1600 hours. No bearing failures occurred related to the restoration by grinding process. The two bearing failures which occurred were due to defective rolling elements and were typical of those which may occur in new bearings. The restorable component yield to the three groups was in excess of 90 percent

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