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Integral throat entrance development, qualification and production for the Antares 3 nozzle

Abstract

Although design analyses of a G-90 graphite integral throat entrance for the Antares 3 solid rocket motor nozzle indicated acceptable margins of safety, the nozzle throat insert suffered a thermostructural failure during the first development firing. Subsequent re-analysis using properties measured on material from the same billet as the nozzle throat insert showed negative margins. Carbon-carbon was investigated and found to result in large positive margins of safety. The G-90 graphite was replaced by SAI fast processed 4-D material which uses Hercules HM 10000 fiber as the reinforcement. Its construction allows powder filling of the interstices after preform fabrication which accelerates the densification process. Allied 15V coal tar pitch is then used to complete densification. The properties were extensively characterized on this material and six nozzles were subjected to demonstration, development and qualification firings

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