slides

Experimental investigation of nozzle/plume aerodynamics at hypersonic speeds

Abstract

An extensive program to improve the operation of the Ames 16 Inch Shock Tunnel was carried out. This included reduction of driver slosh wave amplitudes and detonation risk by the use of premixed He/O2 gas, longer wait times between the last gas load and driver gas ignition, an improved gas loading sequence, the use of four instead of one ignition wire, and the use of lower ignition wire voltages. Successful operation of the tunnel at pressures of 2000-6000 psi and enthalpies up to 12,000 J/gm was achieved. A new diaphragm breaking technique, self break on the driver combustion pressure rise, was tested and found to produce clean breaks over the full pressure range of the tunnel. Improvements were made to the driver gas loading manifold and a preliminary design was made of a gas mixing system which mixes all three gases on the fly just before injection into the driver. Other improvements as well as tests are discussed

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