research

NESC Peer-Review of the Flight Rationale for Expected Debris Report

Abstract

Since the loss of Columbia on February 1, 2003, the Space Shuttle Program (SSP) has significantly improved the understanding of launch and ascent debris, implemented hardware modifications to reduce debris, and conducted tests and analyses to understand the risks associated with expected debris. The STS-114 flight rationale for expected debris relies on a combination of all three of these factors. A number of design improvements have been implemented to reduce debris at the source. The External Tank (ET) thermal protection system (TPS) foam has been redesigned and/or process improvements have been implemented in the following locations: the bipod closeout, the first ten feet of the liquid hydrogen (LH2) tank protuberance air load (PAL) ramp, and the LH2 tank-to-intertank flange closeout. In addition, the forward bipod ramp has been eliminated and heaters have been installed on the bipod fittings and the liquid oxygen (LO2) feedline forward bellows to prevent ice formation. The Solid Rocket Booster (SRB) bolt catcher has been redesigned. The Orbiter reaction control system (RCS) thruster cover "butcher paper" has been replaced with a material that sheds at a low velocity. Finally, the pad area has been cleaned to reduce debris during lift-off

    Similar works