8,059 research outputs found

    A Simulator Study of the Effectiveness of a Pilot's Indicator which Combined Angle of Attack and Rate of Change of Total Pressure as Applied to the Take-Off Rotation and Climbout of a Supersonic Transport

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    A simulator study has been made to determine the effectiveness of a single instrument presentation as an aid to the pilot in controlling both rotation and climbout path in take-off. The instrument was basically an angle-of-attack indicator, biased with a total-pressure-rate input as a means of suppressing the phugoid oscillation. Linearized six-degree-of-freedom equations of motion were utilized in simulating a hypothetical supersonic transport as the test vehicle. Each of several experienced pilots performed a number of simulated take-offs, using conventional flight instruments and either an angle-of-attack instrument or the combined angle-of-attack and total-pressure-rate instrument. The pilots were able to rotate the airplane, with satisfactory precision, to the 15 deg. angle of attack required for lift-off when using either an angle-of-attack instrument or the instrument which combined total-pressure-rate with angle of attack. At least 4 to 6 second-S appeared to be required for rotation to prevent overshoot, particularly with the latter instrument. The flight paths resulting from take-offs with simulated engine failures were relatively smooth and repeatable within a reasonably narrow band when the combined angle-of-attack and total-pressure-rate instrument presentation was used. Some of the flight paths resulting from take-offs with the same engine-failure conditions were very oscillatory when conventional instruments and an angle-of-attack instrument were used. The pilots considered the combined angle-of-attack and total- pressure-rate instrument a very effective aid. Even though they could, with sufficient practice, perform satisfactory climbouts after simulated engine failure by monitoring the conventional instruments and making correction based on their readings, it was much easier to maintain a smooth flight path with the single combined angle-of-attack and total-pressure-rate instrument

    Response of a WB-47E Airplane to Runway Roughness at Eielson AFB, Alaska, September 1964

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    An investigation has been conducted to measure the response of a WB-47E airplane to the roughness of the runway at Eielson AFB, Alaska. The acceleration level in the pilot's compartment and the pitching oscillation of the airplane were found to be sufficiently high to possibly cause pilot discomfort and have an adverse effect on the precision of take-off

    Notch1 mutations drive clonal expansion in normal esophageal epithelium but impair tumor growth

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    NOTCH1 mutant clones occupy the majority of normal human esophagus by middle age but are comparatively rare in esophageal cancers, suggesting NOTCH1 mutations drive clonal expansion but impede carcinogenesis. Here we test this hypothesis. Sequencing NOTCH1 mutant clones in aging human esophagus reveals frequent biallelic mutations that block NOTCH1 signaling. In mouse esophagus, heterozygous Notch1 mutation confers a competitive advantage over wild-type cells, an effect enhanced by loss of the second allele. Widespread Notch1 loss alters transcription but has minimal effects on the epithelial structure and cell dynamics. In a carcinogenesis model, Notch1 mutations were less prevalent in tumors than normal epithelium. Deletion of Notch1 reduced tumor growth, an effect recapitulated by anti-NOTCH1 antibody treatment. Notch1 null tumors showed reduced proliferation. We conclude that Notch1 mutations in normal epithelium are beneficial as wild-type Notch1 favors tumor expansion. NOTCH1 blockade may have therapeutic potential in preventing esophageal squamous cancer
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