31 research outputs found

    Accelerated surgery versus standard care in hip fracture (HIP ATTACK): an international, randomised, controlled trial

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    Impact of carbon to nitrogen ratio and aeration regime on mainstream deammonification

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    While deammonification of high-strength wastewater in the sludge line of sewage treatment plants has become well established, the potential cost savings spur the development of this technology for mainstream applications. This study aimed at identifying the effect of aeration and organic carbon on the deammonification process. Two 10 L sequencing bath reactors with different aeration frequencies were operated at 25 degrees C. Real wastewater effluents from chemically enhanced primary treatment and high-rate activated sludge process were fed into the reactors with biodegradable chemical oxygen demand/nitrogen (bCOD/N) of 2.0 and 0.6, respectively. It was found that shorter aerobic solids retention time (SRT) and higher aeration frequency gave more advantages for aerobic ammonium-oxidizing bacteria (AerAOB) than nitrite oxidizing bacteria (NOB) in the system. From the kinetics study, it is shown that the affinity for oxygen is higher for NOB than for AerAOB, and higher dissolved oxygen set-point could decrease the affinity of both AerAOB and NOB communities. After 514 days of operation, it was concluded that lower organic carbon levels enhanced the activity of anoxic ammonium-oxidizing bacteria (AnAOB) over denitrifiers. As a result, the contribution of AnAOB to nitrogen removal increased from 40 to 70%. Overall, a reasonably good total removal efficiency of 66% was reached under a low bCOD/N ratio of 2.0 after adaptation

    Efficient Total Nitrogen Removal in an Ammonia Gas Biofilter through High-Rate OLAND

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    Ammonia gas is conventionally treated in nitrifying biofilters; however, addition of organic carbon to perform post-denitrification is required to obtain total nitrogen removal. Oxygen-limited autotrophic nitrification/denitrification (OLAND), applied in full-scale for wastewater treatment, can offer a cost-effective alternative for gas treatment. In this study, the OLAND application thus was broadened toward ammonia loaded gaseous streams. A down flow, oxygen-saturated biofilter (height of 1.5 m; diameter of 0.11 m) was fed with an ammonia gas stream (248 +/- 10 ppmv) at a loading rate of 0.86 +/- 0.04 kg N m(-3) biofilter d(-1) and an empty bed residence time of 14 s. After 45 days of operation a stable nitrogen removal rate of 0.67 +/- 0.06 kg N m(-3) biofilter d(-1), an ammonia removal efficiency of 99%, a removal of 75-80% of the total nitrogen, and negligible NO/N2O productions were obtained at water flow rates of 1.3 +/- 0.4 m(3) m(-2) biofilter section d(-1). Profile measurements revealed that 91% of the total nitrogen activity was taking place in the top 36% of the filter. This study demonstrated for the first time highly effective and sustainable autotrophic ammonia removal in a gas biofilter and therefore shows the appealing potential of the OLAND process to treat streams
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